Well of course there’s fire in the burner that’s how it works. After today however the Arduino should be able to sense the fire since I added a photo resistor, commonly known as a flame sensor, bought at a furnace supply store. With the Arduino’s ability to sense flame, the addition of automatic self starting should be enabled. The ability to determine if fuel is building up should also add safety to an already proven safe unit.
The sensor I obtained is a flame sensor used in a normal oil or gas fired burner. The flame sensor allows me to sense the light corresponding to a fire currently burning. The sensor cannot determine if the fire went out or if the flame sensor can no longer see it but functionally it makes no difference to me. I am interested in either condition and the response is the same to both conditions, turn off the fuel feed. If the fire went out, no need to keep feeding fuel, that will simply clog the feed chute and make a mess. If the fuel has backed up the feed chute so much as to shield the flame sensor, there is excess fuel, turn off the fuel feed. Physically the sensor is mounted to “look” through the back of the feed slide. This positions was chosen purposefully to determine if fuel was backing up.
Because the flame sensor is a resistor, I am using a voltage divider circuit to measure the voltage and then using the software to check the voltage with a if – then statement. The software determines if the voltage is high enough to indicate flame or too low indicating dark. I have been recording various sensor data to the micro SD over the heating season, so I will record the voltage overnight and we can see the range of data tomorrow. If anything this should be a good time of year for the test since the fire is needed to maintain the temperature in the building, it is mid 30’s F here today, but the fire is not required to be too vigorous since the temperature is not extremely cold.
Pictures and data to follow.
It may not be cabin fever, more just a general malaise. That midwinter everything is working and I don’t want to take it apart feeling. But I have several projects half done at this point. I am waiting for headers to install the Ethernet card so the Ethernet update project is on hold. The CNC plasma cutter is apart awaiting a new lead screw for the y-axis. This is to remove the vibration issues I have been experiencing. I am changing from a single start to a five start lead screw. I will lose one fifth of the resolution I have presently but that will still be plenty of resolution for this application. But the big news is I am finally going to move on building a new firebox. It’s time to retire the over the road fuel tank turned boiler. Well maybe not retire, just move onto a new home. Anyone want to buy this working boiler? I would consider selling the auger and burner feed as well as a combination. The unit is located in Newport, NH if you would like to see it working. It won’t be available until it’s replacement is built. It is after all heating the house, shop and hot water. But I am hoping to have the replacement built before the end of the heating season for some testing. If you are interested drop me an email at: email@example.com
A quick reminder of what the combination looks like, this has successfully burned pellets, chips and to a limited degree sawdust. Ideally you would be a person who can tinker as this is a prototype unit.
The software, Arduino and LCD display all very solid and work very well.
The PID control continues to work great, after 3 1/2 days the PID seems to be in good control. The graph shows a bit of variation but within 10 degrees which seems within bounds.
During this time period I used an average of 2.15 bags of pellets per day. At 40 lbs. per bag this is 86 lbs per day or 39.09 kg/day. At a cost of $216/ton. this is $9.28/day. I am hoping to reduce this to less than a dollar with chips but before I do, I intend to implement some more mechanisms to reduce fuel usage. More to come with the new year, Merry Christmas, Happy Holidays everyone.
I rebuilt the burner yesterday added more air holes in selected areas and tried to stop up the misc air leaks to see if that
would add more power. I’ll let the graph speak for itself. Note the issue at 45 or so minutes in where the temperature started to drop. At this point the sawdust bridged so badly it wasn’t feeding any fuel. After I poked the sawdust in the hopper, the temperature continued to rise. I had to continue to poke the pile to get the feed rate to be somewhat normal. Looks a lot like yesterday’s graph, so I am thinking about adding some additional air through a forced draft fan on the front end of the process. Once again the burner did do the job but slowly and until approx. 379 minutes or a little more than 6 hours into the test did the temperature rise past the point where the circulator turned on. I measured the chamber pressure, in this case vacuum and it measured .1″ H2O so additionally I am wondering if I need a larger exhaust fan as well.
Over the summer and fall I have written and tested a number of programs to have the building blocks of a working program. I knew the key this year would be the ability to log data. Of course to log data and have it mean something you have to have good data. So I spent several days working the bugs out of OpenLog, which works but I would not recommend. I also spent some time figuring out a combination of moving averages which resultx in stable data.
Of course the integration process was a train wreck. The arrays used for moving average data smoothing were declared wrong so that bug had to be found and fixed. The Serial LCD needed to be replaced, and my soldering iron wouldn’t work. A few of the functions are timed and there were some issues with those functions. The code for Open Log was not robust enough, once I worked out all those issues, which took most of the weekend, it is finally ready to test.
I had a plow in the shop for repair and soaked up the spilled hydraulic fluid off the floor with some sawdust, actually pellets that got wet. So the hydraulic oil soaked sawdust is in the hopper to be burned. It’s burning now, so tomorrow I should have some excel data which will help me make decisions to improve the software. At this point I am not sure it will be valid however, it is really taking a long time to come up to temperature with the sawdust. Another data point.
It took me longer than I would like, but the hopper/auger assembly is now painted and the electrical box is mounted and the wiring is functional. I have mounted the Arduino and LCD display. That box also contains the board that accommodates the thermistor electronics, which are the sensors that read various temperatures.
The main electrical box is a stainless steel box I picked up used from a scrap yard, putting the frugal in frugaltinker.com. That’s the reason that there are so many holes in the box, however it was such a good deal I thought it was worth it, despite the cosmetics. The cover was just too ugly to leave be, so I attempted to skin the cover with a plate which I plasma cut in “Frugaltinker.com”. This doesn’t show up too well, I probably should paint a background behind it to make it stand out better. Painting a background seems low on the to do list right now, so I think I will skip that task and focus on the burner.
The CNC was invaluable in the production of the electrical mounting plate, mounted inside the electrical box. It was great to not have to drill any holes to mount anything. All the holes were cut with the CNC and fit just fine.
So the final task is complete before the burner is welded up and tested.
I often have to cut multiple parts, so when I do, I take the opportunity to experiment a bit. In this series of cuts I changed the amperage of the Plasma cutter, a Hypertherm 45. Hypertherm plasma cutters are American made, designed and built, only about a 45 minute drive away from me. I still haven’t gotten my free T shirt for buying and registering the machine but I guess that’s another story… anyway, amazingly enough there really is not a lot of difference in the dross or slag between the three different amp settings I tried. I’ll keep experimenting to try to optimize the cut quality and speed of the CNC machine, plasma cutter combination.
The auger pipe connects the burn plate which attaches to the boiler and forms the interface between the auger feed and the boiler/burner units. I took a piece of 6″ pipe and welded it to the boiler plate and this attaches the plate to the auger feed via screws that tighten. With this assembly I can detach the auger and hopper and test a different burner simply by loosening 6 screws. Modular design for ease of design changes and maintenance.
I attached the hopper plate first because this determines the wheel height required. I slotted the holes in the saddle plates so that there is about 3/8″, or about a centimeter of adjustment up or down adjustment. Then after careful alignment I assembled the entire assembly with clamps and threaded rods. I did cut and weld in some cross pieces with gussets
This will make maintenance of the boiler, ash removal, scraping of the burner holes, boiler tube cleaning very easy by simply rolling the auger/hopper assembly out of the way.