At this point the boiler has been working for a day and based on last years experience I see no reason why I would need to shut down for a week. Yesterday we brought two tons of pellets into the shop knowing snow and rain mix was in the forecast. Yesterday was a pleasant 40°F day with full sunshine a great day to move a little fuel. I believe we are on a two bag a day pace so with luck I won’t have to worry about moving pellets again until nearly February. We have chairs set up by the boiler and it is a pleasant place to sit and talk in lieu of sitting in front of a woodstove.
So..what’s next on the list. 1) Software improvements, to be able to adapt to pellets or chips will take a more dynamic software approach. The software should be able to adapt automatically to varying energy densities. 2) Faster and easier maintenance. More over center latches to be able to easily take apart the chimney for cleaning and a removable top to the boiler to easily clean the tank tubes. 3) Testing with various materials, chips being at the top of the list. 4) Building a chip dryer. 5) Adding more sensors, I am definitely going to add a fire eye to confirm fire. I would like to monitor the temperature of the feed motor and the fan motor. It would be helpful to add a relay for the fan motor so that is controlled by the Arduino. 6) I have tried the self start but it is not in the software yet, that would be a great leap forward especially for March and April when daytime heat is often not required but nighttime heat and hot water are needed. Automatic starting would be great and would save a lot of fuel. 7) Improving the CNC Plasma cutter, there is still some chatter in the Y axis and if I can fix that, it would be great and would probably speed the CNC up significantly cutting down on the dross or slag produced when it is cutting. Cutting down on the slag is a major priority since it is time consuming to grind this off and I am sure part of the development will include trying different burner designs. 8) Taking a Design of Experiments statistical approach to the burner design to optimize for efficiency. I gave myself a pretty good list back in September and I have whittled it down to completion so I know it is all possible and fun, I just need to get started. Tomorrow probably, today I am just going to sit by the fire and enjoy a Sunday.
I added gasket rope which I bought at a local hardware store, which is made to replace the gasket material which comes in a wood stove door between the burn plate and the boiler. This gasket changed the Magnehelic vacuum reading from .1″H2O to .4″H2O. That I thought would make the flame a bit more vigorous. I also made the holes in the bottom of the burner larger to allow the ash to fall through. Lastly I made minor changes by tacking some material across some holes and making more air holes in the ramp plate which the pellets fall down.
The main differences in this graph and the previous day’s graphs are at approximately minute 273 pellets were added and the sawdust which had been running finally ran out. As you can see it had enough energy density to overcome the demands of the circulator circuit. The biggest problem after that came at about 341 when the program allowed the temperature to go past the set point of 140°F The only explanation I could come up with is the division by different types of declared variables was not allowed and yielded a result of zero. I was dividing an unsigned long which is an integer by .8 to increase the Auger Off time by 20%. Since you will not get an integer when you do this the program may not have liked this result. The Arduino language is a slight variant of C++ . I have since made all the variables doubles we’ll see if that works. Today’s burn will be a better test of the burner floors ability to let ash fall through. Sawdust is very difficult to burn. It’s also difficult to get the ash to fall through the burner floor. I think this is because the air cannot get around the sawdust sufficiently to burn it completely and hence it smolders in clumps instead of falling through the grate. The burner when I pulled it out to inspect it was definitely not clean of ash but did appear better than yesterday.
I rebuilt the burner yesterday added more air holes in selected areas and tried to stop up the misc air leaks to see if that
would add more power. I’ll let the graph speak for itself. Note the issue at 45 or so minutes in where the temperature started to drop. At this point the sawdust bridged so badly it wasn’t feeding any fuel. After I poked the sawdust in the hopper, the temperature continued to rise. I had to continue to poke the pile to get the feed rate to be somewhat normal. Looks a lot like yesterday’s graph, so I am thinking about adding some additional air through a forced draft fan on the front end of the process. Once again the burner did do the job but slowly and until approx. 379 minutes or a little more than 6 hours into the test did the temperature rise past the point where the circulator turned on. I measured the chamber pressure, in this case vacuum and it measured .1″ H2O so additionally I am wondering if I need a larger exhaust fan as well.
If last years burner was a vehicle it would have been a freight train, powerful and hard to throttle back. This new burner is a Jeep, dependable and at at this point slightly underpowered. The burner design will no doubt need to be tweaked but it was a great first day. As you can see the burner was having a hard time getting well lit. Those of you with a wood stove I am sure can relate. At about 118 minutes in the flames finally took over and the slope looks good.
The saw tooth effect you see up top is the result of the circulator pump turning on and off. I turned up the thermostat on the shop floor which has radiant tubes so this was a big load and it did not have the power to overcome the load. Although from the frequency change at the end you can see it was starting to catch up. But I am going to redesign the burner to direct the air flow a little better.
Over the summer and fall I have written and tested a number of programs to have the building blocks of a working program. I knew the key this year would be the ability to log data. Of course to log data and have it mean something you have to have good data. So I spent several days working the bugs out of OpenLog, which works but I would not recommend. I also spent some time figuring out a combination of moving averages which resultx in stable data.
Of course the integration process was a train wreck. The arrays used for moving average data smoothing were declared wrong so that bug had to be found and fixed. The Serial LCD needed to be replaced, and my soldering iron wouldn’t work. A few of the functions are timed and there were some issues with those functions. The code for Open Log was not robust enough, once I worked out all those issues, which took most of the weekend, it is finally ready to test.
I had a plow in the shop for repair and soaked up the spilled hydraulic fluid off the floor with some sawdust, actually pellets that got wet. So the hydraulic oil soaked sawdust is in the hopper to be burned. It’s burning now, so tomorrow I should have some excel data which will help me make decisions to improve the software. At this point I am not sure it will be valid however, it is really taking a long time to come up to temperature with the sawdust. Another data point.
It took me longer than I would like, but the hopper/auger assembly is now painted and the electrical box is mounted and the wiring is functional. I have mounted the Arduino and LCD display. That box also contains the board that accommodates the thermistor electronics, which are the sensors that read various temperatures.
The main electrical box is a stainless steel box I picked up used from a scrap yard, putting the frugal in frugaltinker.com. That’s the reason that there are so many holes in the box, however it was such a good deal I thought it was worth it, despite the cosmetics. The cover was just too ugly to leave be, so I attempted to skin the cover with a plate which I plasma cut in “Frugaltinker.com”. This doesn’t show up too well, I probably should paint a background behind it to make it stand out better. Painting a background seems low on the to do list right now, so I think I will skip that task and focus on the burner.
The CNC was invaluable in the production of the electrical mounting plate, mounted inside the electrical box. It was great to not have to drill any holes to mount anything. All the holes were cut with the CNC and fit just fine.
So the final task is complete before the burner is welded up and tested.
I built a homemade brake to bend sheet metal and it works OK, not great. The corners are really radius’s and fairly large ones at that. The second and main issue I have with it, is the inconsistency that comes from the bends. I find that even though I try to align things perfectly it does not work that way. Some of the parts I have made lately I have cut some slits with the CNC to weaken the folded edge making it more consistent and I wish I had done this for this part of the project….Anyway, a quick reminder of last years effort.
As you can see the hopper is quite small and I ended up adding an extension later. The burner is integral to the hopper and auger, making it very difficult to make any changes to the burner. Lastly the legs are welded on and have no adjustment and seriously two wheels what was I thinking? So while the principal is the same there are some major differences.
It’s pretty challenging to align four pieces of steel of such odd shapes and weights, so in this iteration I cut some gussets with tabs to fit into a slot in the end pieces of the hopper. This keeps the end pieces fixed from side to side because of the slot and plumb as it is butted up to the square the gusset forms. All from welding a gusset plumb. So that was an aid to success, of course as soon as I finished I tossed some ideas around with a friend and we thought up a perhaps better way by making two peices instead of four and doing a different bending technique. Next time. In the meantime this is straight, level and functional. Almost done with the hopper/auger assembly, The last task is to mount the electrical box and paint the entire assembly while it is still apart and then assemble it into a working machine and test the auger drive.
I often have to cut multiple parts, so when I do, I take the opportunity to experiment a bit. In this series of cuts I changed the amperage of the Plasma cutter, a Hypertherm 45. Hypertherm plasma cutters are American made, designed and built, only about a 45 minute drive away from me. I still haven’t gotten my free T shirt for buying and registering the machine but I guess that’s another story… anyway, amazingly enough there really is not a lot of difference in the dross or slag between the three different amp settings I tried. I’ll keep experimenting to try to optimize the cut quality and speed of the CNC machine, plasma cutter combination.
The auger pipe connects the burn plate which attaches to the boiler and forms the interface between the auger feed and the boiler/burner units. I took a piece of 6″ pipe and welded it to the boiler plate and this attaches the plate to the auger feed via screws that tighten. With this assembly I can detach the auger and hopper and test a different burner simply by loosening 6 screws. Modular design for ease of design changes and maintenance.
I attached the hopper plate first because this determines the wheel height required. I slotted the holes in the saddle plates so that there is about 3/8″, or about a centimeter of adjustment up or down adjustment. Then after careful alignment I assembled the entire assembly with clamps and threaded rods. I did cut and weld in some cross pieces with gussets
This will make maintenance of the boiler, ash removal, scraping of the burner holes, boiler tube cleaning very easy by simply rolling the auger/hopper assembly out of the way.
In this step I mount the auger drive motor, it has a built in right angle drive and speed reducer which adds torque. The motor comes complete ready for wiring and mounting using four screws. Again I drew up the parts in SketchUp and then cut them out on the CNC plasma cutter, it was almost too easy. The further I get down this path the more I take advantage of the CNC’s capabilities. Note the rounded corners, I also added an extra hole on top of the motor mount plate to make adding a wire routing clip easier in the future. I remade the worm drive plate to improve some of the adjustment capabilities and added at the same time some decoration, rounded corners and used less material.
I used a Lovejoy type shaft connector to connect the motor to the worm shaft with a Buna-N spider in between to minimize any vibration or backlash to the motor, although with the worm and worm gear combination there should be none.
This step was made simple by the use of the CNC plasma cutter to make a part which I then bent up on both ends using my homemade brake. But first let’s revisit the old configuration for comparison.
I had to rob the motor and some parts from this transmission so it is in disarray but you get the idea of the complexity. It requires four sprockets, two chains, a motor and two chain tensioners. Here is a picture of the newly implemented and untested solution for mounting the worm and worm gear.
The CNC made it easy to slot the holes for adjustment, so the vertical adjustment comes from the plate to plate mounting screws, and the bearing mounting holes are slotted to get correct in and out adjustment to the keyed worm. After cutting the part and mounting it I decided what to change in the next iteration. I modified the part to round all the corners so that there are no sharp edges and extended the plate to pick up a second set of holes so the plates are attached with four screws instead of two. I think this part is perfectly functional so I won’t implement the changes but at least the SketchUp drawing has been updated.