Changed feed sprocketPosted: January 4, 2012 Filed under: Arduino, Homemade Boiler, Hopper and Feed, LCD display | Tags: Arduino, Arduino boiler control, auger feed, Auger motor, boiler, lcd display, LCD problems, pellets, relays, run time, shaded pole motor Leave a comment
The New Year practically demands resolutions and change for the better. So with that constant improvement theme in mind I am publicly stating my goal to lose 15#’s and so I am starting from 195.7. My second resolution is the constant improvement of the boiler. So here we go……
Auger feeding failure due to the motor stalling demanded the sprocket change on the auger motor feed assembly. The sprocket I chose doubles the torque available for feeding pellets. Since the shaded pole motor is constant speed the program had to change to double the auger run time. So taking the data I had gathered I changed the program in two ways.
I changed the times to accommodate the speed change demanded by the sprocket change and I changed the paradigm to have constant run time and vary the dwell or off time. The increased torque is a vast improvement and since the change it has had no problem feeding even adding an entire bag of pellets at one time.
A second advantage of the change is the improvement of the LCD display. I think that this problem is now fixed since the LCD has been running without garbling the characters for several hours, long past the time when the LCD would normally have failed. By increasing the torque the auger feed motor is running at less amp draw and so it feeds back less to the relays. I also grounded the relay in a more positive way.